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SHEAR (ASTM A-1056)

Two 5 foot lengths of randomly selected hubless cast iron soil pipe were joined with an MG COUPLING, torqued to 175 inch-pounds, and the ends of the assembly were sealed with test plugs. One pipe was rigidly supported while the other was supported by a single block near the end of the pipe. The assemble was filled with water and the hydrostatic pressure was held at 4.3 psi for the duration of the test. A load of 50 pounds per inch of nominal diameter of the pipe was uniformly applied over an arc of 120 degrees and along a longitudinal distance of 12 inches at the unsupported end of the pipe immediately adjacent to the coupling and held for 15 minutes. Test required displacement not to exceed 0.375 inches from true alignment and no leakage.  
MG COUPLING (sizes tested) Shear (pounds) Displacement (inches) Results
1½" 75 0.018 No Leakage Occurred
1½"x 2" 75 0.024 No Leakage Occurred
2" 100 0.017 No Leakage Occurred
3" 150 0.019 No Leakage Occurred
4" 200 0.029 No Leakage Occurred
5" 250 0.030 No Leakage Occurred
6" 300 0.031 No Leakage Occurred
8" 400 0.055 No Leakage Occurred
10" 500 0.080 No Leakage Occurred